Well, that was a nightmare!
As you saw from the earlier photos I had previously fitted a Toyota W58, 5 Spd gearbox. This, together with the adapter plate, is about a foot longer than the standard box, and bulkier. When I fitted the engine, I built the engine frames around it to avoid the heavy lifting. No problem, it worked like a charm. Getting the bugger back out again was another issue.
I have a one-post ramp so I tried dropping the engine down and lifting the car - no good - even with all the pulley's and water pump off. I tried lifting it up and over - no good. In the end the only way it would come out was by dismantling the picture frame/suspension/steering and lifting it on a shallow incline to clear the tunnel and the lugs on the lower front engine frames. By then of course I had stripped the engine of its carbs and manifolds etc etc. A pile of work I hadn't foreseen. I think the car hates me!
Anyway, back to the clutch, what I found was a combination of your suggestions above. Thanks to those who supplied measurements. My Toyota clutch plate was about standard to the jag one so no problem there, but the flywheel was about 2.0mm thinner than standard. My fitted thrust bearing was identical to the new one I ordered so I located another that was about 3mm deeper, (the casting was the same but there was more carbon on it). I also could see that the fork would foul the adapter plate (which is about an inch thick) at the end of its travel so I gave this some significant surgery so that the fork will now travel all the way back until it hits the housing, if required(?).
I checked the throw on the starter driving gear and there was 2 mm spare so I ordered an extra flywheel tab washer and fitted this as a spacer behind the flywheel. This almost made up the difference. I tested the flywheel with a dial gauge to make sure it was all true. Perfect!
I also replaced my horrible rusty slave push rod too.
Anyway, I have put it all together. The clutch lever is in what looks like the correct position now. I tested the clutch while the engine was on the floor with a couple of spare meters of pipe. It was considerably easier. While I was doing that, I tested it with and without the rather robust return spring that a few of you commented on. It was noticeably lighter without it - not in a major way but you could certainly feel it in your foot. I stretched the spring slightly so that it still worked but was slack at rest, another slight improvement.
While I was at it I also fitted a spacer on the clutch master cylinder to lower the pedal as it towered above the brake pedal in the footwell. This worked well and there is still room under it when the clutch is fully engaged.
So the engine went back in in just a few minutes and I am now refitting the picture frame etc. What a saga, but I think worth fixing it now rather than later. I would never have been happy with it.
Thanks for all your help, particularly Steve, Tadek, Steve 3.8, Andrew and Marek and the other contributors. I really appreciate your advice and help.
My best regards
Steve
