Initially thought that it was a faulty oil pressure gauge but soon confirmed that is wasn't so decided to drop the sump and this is what we found

Then investigated further and found what had happened to the oil pump.

Then the crankshaft,

Turns out that, the crankshaft thrust washers had been fitted the wrong way around, had broken up and been eaten by the oil pump !


Smashed oil pump :(



Turns out that when the car was rebuilt in America before I bought it, the engine had been rebuilt with the crankshaft thrust washers fitted the wrong way around.
End result is we still don't know for sure what other damage has been done to the rest of the engine till it's stripped, so have decided to send it for a full rebuild with CMES, so will let you know what they find out in a few weeks time ?








